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george 1100

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Everything posted by george 1100

  1. I contemplated converting mine to side pull just for ease but not sure if it will fit. At the moment the centre pull cables interfere with the oil take off bar at the rear of the valve cover
  2. Usually when they don't flow on prime it's because the cast alloy ramp of the centre part that turns, has worn out. They are in general good units but if you use the prime feature often, the cast alloy wears out real quick
  3. It's a switch in the normally closed position so when there is no oil pressure it's a closed circuit and oil pressure light is on. When oil pressure builds, it opens creating an open circuit and light turns off
  4. I put oversized valves and stage 2 yosh cams in my 1277 and lightened the crank and rods(Hayabusa). Runs very strong , super responsive. Cams are dialed in at 102/105 I only rev it to 10k
  5. That's very common. Most looms I've seen have that exact problem in varying degrees of failure
  6. I tried an 2012 1000 basket and it just interfered with the rod. There earlier 1000 may fit as they have a slightly different shape on the outside of the basket but I don't want want to spend the money to find out it won't. Shaft length was also an issue
  7. Maybe it became an issue so on the later 750, they re-engineered it. Every photo I've seen of 85_86 cases has a hole
  8. If you are at the limit of your tensioner then your chain is operating beyond the manufacturers spec
  9. Similar thing thing happened to me. Bought a set of used rs40s but didn't try them for over a year so couldn't return them. Discovered pilot had broken off and become wedged and no matter what I tried, I couldn't remove it. The cost of a replacement body outweighed the cost of buying a new set. The only thing I didn't look into was to get someone specialised to drilled it out but again, the cost would've been high. I ended up selling the set as is for surprisingly not bad money and bought new
  10. I'll bet you had a tiny bit of grit stuck in the needle and seat. Fouling your plugs at idle but running good at open throttle with 145 jets. The grit now gone . Doesn't explain the plugs with 130 jets though
  11. I had a problem similar to this with NGKs and the thing is, you assume they're working 100% because they're new, so you set off on a goose chase, driving yourself insane until you come full circle and realise the new plugs you put in were no good
  12. Personally I wouldn't run that head like that. Those cracks are decent which could lead to the seats falling out. The cost to fix properly would outweigh the cost of the head. Shortcut repair would be to weld up as is but the risk remains
  13. Zx10 work also but can't remember the year. There was a list of coils on the net somewhere with ohms noted.
  14. I was waiting for that. Absolutely no chance of metal to metal even after a minute of idle
  15. I drop the oil then run the engine on idle for about 5-10 seconds to get most of it out
  16. The oil cooled engine was undervalved imo. It's the single best mod with a compatible port job, you can do. Expensive though
  17. Correct but the 750 spring cannot be used with the ST2 10mm lift cams as they will coil bind
  18. 38mm flatslides Basic port job focusing on cleaning up the bowls, short turn and blend and port match 80mm 12:1 pistons instead of spending on cams Slotted cam sprockets No need to skim anything That should comfortably bump you over 130hp. Unless you are chasing big numbers, don't waste you're time with big valves and dot heads imo
  19. I'm just about to make one up for my track slabby but am using a different cowling. Mine will need to support a head cooler also. I'll post up pics. Take yours to a competent fabricator and they should be able to knock one up easy enough
  20. ⬆️ this and to dissipate heat from valve springs
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